Showing posts with label permanent magnet. Show all posts
Showing posts with label permanent magnet. Show all posts

Wednesday, December 28, 2011

Sunbeam S7 / S8 permanent magnet alternator conversion (recap)

This is a recap of my alternator build.
(as published in the Sunbeam Owners Fellowship club magazine "On The Beam" issue Nov-Dec 2011)



I’ve been frustrated with the original Lucas dynamo on my Sunbeam since I’ve been riding it. Neither the MC45O nor the MC45L (that I later purchased) produced enough electricity in a foolproof fashion. I don’t want to have to worry about if there’s enough charge in the battery to get me home anymore, and I want to run the lights all the time. I also don’t want an after-market alternator conversion that does not look exactly like the original. This is why I was determined to create an alternator conversion by myself for a small price. I submit the following to any interested do-it-yourself owners.
I took suggestion from some Douglas and Vincent motorcycle owners who also have problems with dynamos. A few intrepid owners have taken permanent magnet alternators from modern applications and fit them inside the original dynamo cases. One particular application caught my eye while searching online for a suitable solution. There is a simple alternator from a Kubota tractor that measures only 3-1/2” across and a little over 3” high. I bought model APM0001, which was the smallest available. This came as a self-contained belt driven assembly. I tested it briefly before taking it apart to see how easily it produced enough current being turned by hand to light the tail lamp bulb on my bike. Removing the nut and pushing the bolt out easily disassembled the unit, shown in Figure 1. The back housing was discarded.

Figure1

The magnet cup was surprisingly powerful. It all fit nicely into the original dynamo case. There would be two major challenges. Fit the magnet cup to the crankshaft, and then to fit the case back onto the engine block so it all stayed together. I elected to do the reverse of what the Douglas owners had done, and fit the magnet cup onto the shaft first, so that the stator would be accessible from the front of the bike. It sounded wrong at first, but it eliminated so many problems it was worth the effort, in my mind, to machine all the required parts on the lathe. There would have to be an adapter to fit to the end of the crankshaft, which included pins to fix the magnet from rotating independently from the crankshaft. This I spun out of round stock on the lathe to a relatively high degree of precision. I would use the original left-handed bolt so I didn’t have to machine another one. The outside casing would have to be secured to the engine block by means other than the two long bolts originally used, because they interfered with the outside diameter of the magnet. The wires could easily come out the front and affix to the original terminal block. Below is the solution showing the framework cage that was made to hold the outside casing. I could have welded tabs to the casing, but I didn’t want to modify it.
Figure 2

The whole assembly fits together with a specific procedure, it’s not ideal, but it works. (I later discovered that the magnet was so strong, that I needed to fit two of the sealed bearings inside the stator winding assembly to keep it centered with respect to the crankshaft. That isn’t represented in the photographs.)

The cage, at the left of Figure 2, goes on first. The magnet and center bolt (with spacer) then affix to the crankshaft adapter. The spacer holds the sealed bearings from the original Kubota unit, and another outside press-fit spacer makes up the difference between the stator and the outside bearing race.  The fourth arm of the cage assembly encloses the magnet, before the case is slid onto the cage. The pole shoe screws fasten the case to the cage in such a way that it forces the case into the engine block firmly as the countersunk screws are tightened. The stator coil, at the right side of Figure 2, slides into the magnet which is centered by one of the bearings from the original alternator assembly. This took a brass spacer precisely machined out of an old pipe fitting. The wires tuck neatly up against the casing out of the way of the rotating magnet. The outer plate bolts on with 6 screws and then the cast aluminum cover of the dynamo bolts to the outside of the case.




Figure 3

I’m quite pleased that the mechanics of my alternator conversion work well. The next challenge was to rectify and regulate the alternating current into direct current. Normal people would just have converted to 12 volts and put the Kubota tractor regulator in place of the Lucas MCR2 dynamo regulator. I had purchased a Rooster Booster 6 volt positive ground ignition module, and already had my 6 volt battery and lamps, so I was determined to stay with 6 volts for the present time. I know it’s not ideal, but I knew I could make it work fine. The 6 volt scooter rectifier/regulator that I bought was quickly overwhelmed by the 14 amp capacity (and probably the open circuit voltage capability) of the stator coil, and burned out. I ended up with a commercial shunt regulator from Electrex World LTD.

I spent a lot of time on this project, but it met my goals. It looks original from the outside, it is reliable, and it was less expensive than the alternatives, as long as I don't count my massive investment of time.

Keep Shafting

Wednesday, July 6, 2011

Alternator - Proof of Concept

I'm fed up with the original Sunbeam S7 Lucas dynamo, and the MC45L dynamo that I bought. Neither one produces enough electricity in a foolproof fashion.
I don't want to have to worry about if there's enough battery to get me home anymore, and I want to run the lights all the time. I also don't want an after-market alternator conversion that does not look like the original.

The plan is to create an alternator conversion that produces 6 volts, is fully encased in the original housing, and works reliably.

I've seen others who have used a Kubota tractor permanent magnet alternator to do the job. Its only 3-1/2" in diameter and shorter than the MC45L dynamo. That means it should fit inside the casing. The trick is to mount it up.



It comes as a flange mount unit for belt drive, with its own bearings.

[edit]  I actually did use the bearings after all to keep the stator assembly centered in the magnet.  The magnetic forces are VERY strong radially, and will pull the stator into the magnet if there is the slightest mis-alignment or looseness.  A spacer piece was machined to hold two of the bearings into the stator and then the bearings were placed on the center bolt with their own machined spacers.

The permanent magnet rotor can attach directly to the S7 engine crankshaft, and the stator can mount to the engine block, or dynamo casing. All that is critical is that it runs centered and true. Should not be a problem for a guy with a lathe in his workshop.

Here's the sample fit up.  The center bolt presses out of the rotor cup easily.  This will allow me to make a bolt (left-handed Whitworth of course) to fit in there and mount to the crankshaft.  The question is whether 'tis better to bolt the stator to the engine block, or to bolt the stator to the outside of the dynamo, and put the rotor cup "upside down" against the crank.  I'll have to make an adapter to provide the seal to the front of the engine regardless.  The stator to the front makes it easier for the wires to come out to the terminal block on the dynamo casing.


The final part is the regulator / rectifier from a scooter.  I've bench-tested the rectifier / regulator up to 6 amps load.  It works fine with 14 vac input, and does not overheat.

Here's a VERY ROUGH sketch of the assembly.  I keep changing the design, so my dimensioned sketch is pretty bad.  I will require a minor modification to the dynamo case.  The cap screws will interfere with the side of case, so the case will need to be ground away in two small spots not visible from the outside.  The cap screws can be modified slightly to reduce the amount of grinding to the case.